23.09.2022, 09:03
Hello, going back to this incident... in the image of the KNX bus statistics it can be seen that the load is minimal.
This is for the control of an elevator and practically all the objects associated with the control logics are virtual, being used at most between 5 -8 knx objects for a maneuver.
This works perfectly and sometimes depending on the time at full capacity without rest, and these alerts are not detected. But at some point, without explanation, the bus is blocked and therefore the elevator does not work.
I have seen that it is solved by connecting remotely and executing an order directly in LM or even from the mosaic view.
This is on an LM Reactor updated to the latest version.
This is for the control of an elevator and practically all the objects associated with the control logics are virtual, being used at most between 5 -8 knx objects for a maneuver.
This works perfectly and sometimes depending on the time at full capacity without rest, and these alerts are not detected. But at some point, without explanation, the bus is blocked and therefore the elevator does not work.
I have seen that it is solved by connecting remotely and executing an order directly in LM or even from the mosaic view.
This is on an LM Reactor updated to the latest version.